How I fixed IWC Pilot's Chronograph cal 630 - with a self-made magnetic coil

IWC Pilot's story and tech info

I decided to write this article because I didn't find any solution to this problem on the net :) or maybe nobody has written about it yet.
Some time ago, I won an IWC Schaffhausen Pilot's ref. IW3741 in the online auction. This watch has a so-called mechaquartz (meca-quartz) movement. Calibre 630/1 was developed by Jaeger-leCoultre in 1987 (this movement was also used by IWC). 
Mechaquartz is a hybrid movement - because it has a mechanical chronograph module. According to the description, the watch was "in working condition". When I got it, it turned out it works only partially - the chronograph module doesn't work 😡😤. 

IWC Schaffhausen Pilot's Chronograph ref. IW3741. Jaeger-leCoultre Calibre 630/631 data: meca-quartz 25 jewels, 233 components, 2 stepping motors 1Hz timekeeping, 4Hz chronograph module, moonphase module (only 631).

The winning price for this item was quite good - about $0.5-1k cheaper than in usual "buy now" offers. But sometimes, an auction is a risk or a challenge - like in this case.

Diagnosis - Why it doesn't work?

I decided that I could handle repair "by myself", having this amount of saving in my pocket. I have some non-professional experience in watch servicing (hobby). I opened the case to look at the movement. It turned out that the chronograph magnetic coil connector was broken - actually, there was no connector inside! So, it couldn't work. There is no connection between the wire coil and the movement circuit board without this part. It also means that the chronograph wire coil is damaged. Somebody (a big watch seller with an excellent rating) didn't check chronograph functions or made a mistake in the item description. 

The wire coil is damaged, and there is no connector attached to the wire coil.

There is a visible trace of connector removal.

The missing connector (that should be attached to the coil) looks like this. 

Genuine parts issue

I started searching for the proper wire coil replacement for the Jaeger-leCoultre calibre 630/1 (631 contains a moonphase module). And guess what... there is ZERO available around the world - there was only something on the web archive that was SOLDOUT. After this disappointment, I decided to buy complete movement. It is not easy because the coil is often broken in so-called "for parts" offers. The price for an entire working movement is around the watch price.  

Trying to adjust foreign parts.

So I decided to find an "alien" donor of parts, take out the donor's magnetic coil, adjust the coil handles and install it in the calibre 630. In theory, this could work. The calibre 630 chronograph motor doesn't require much induction power to rotate. If the coil fits inside, it will work. Like other quartz movements, this one contains a levet-type stepping motor (Wikipedia).
It turned out that it is pretty difficult to adjust/resize coil handles and not damage them.
A first donor circuit board with an integrated (size-similar) magnetic coil: 

Liquid silver connection points at the wire coil surface.

I had already attached the ends of the wire to the liquid silver (conductive adhesive). So, I created "connection points" directly on the coil surface. I used an eyeglass to be able to disconnect wire ends from the circuit board and move them to the liquid silver. Conductive adhesives are often used when soldering is not an option.
I made a small "reshape" of the left handle to fit the original IWC coil mounting. I also painted the coil to isolate wire:

The replacement is slightly fatter than the genuine coil. The original IWC/JLC wire coil is extremally thin it is hard to find something close to its diameter. 

The connection to the watch circuit board is made with liquid silver (conductive adhesive). This is not permanent - silver could be easily removed from the circuit board:

The replacement barely fit into the movement. 

Eventually, everything fit in the watch case.

After putting all together, it was working! I recorded a short video with this great success:

Unfortunately, the joy did not last long.

... It was working, but only for about 3 hours ☹️ - after 3 hours chronograph started to slow down and finally, it stopped. There was a short circuit (in the coil). The donor coil was already pained I was not able to repair it. Even without paint, it is hard to fix a wire coil.
Then, I decided to try another donor: 

But this one had developed a short circuit during installation and didn't work. 

Making a watch magnetic coil

So after several attempts with different donors, I give up. After some hard thinking, I decided to use the donor coil differently - I need only a proper wire and an original coil core! 

But how to wind wire (much thinner than a human hair) without 10k$ winder stuff? 

I found a possible solution. Even a thin wire should be strong enough to survive the rewinding process. The strain on the wire causes the source coil to unwind. I browsed the net to the end and found a wire coil that is easy to un-wind (the coil without a protection layer on the surface) - Miyota GL20 or GL30 is a good match. I bought several for $2.5 each:

Miyota GL30 with coil wire without a protective layer is a good source of enamelled copper wire.

I don't have a professional winder, but I have an excellent Makita drill with smooth movement control, watchmaker mounting stuff (pin vise), and my re-winder PoC (proof of concept):  

Donors small watch magnetic coils with proper wire and a bigger one (from quartz clock) used as a source of isolated output wire.

During rewinding, I used a paper towel as a tension balancer. The rewinding process takes (with pauses) about 25-40min (with a max of 2-3 turns per second). It is essential to be focused during the process - movements should be languid (from left to right coil edge) to create similar wire layers. It is tough to see wire after a while of rewinding (maybe a zoom screen would be a good option).

(1) The donor coil is attached to the elastic filament - It is possible to adjust it, making the unwinding process much more manageable. (2) The strain on the wire causes the source coil to unwind.

(1) Makita drill is used to wind a new wire coil. The pin vise is connected to the drill and is used to hold the coil core. (2) A Paper towel is used to reduce tension and move the wire from left to right. 

The first re-winded coil looks like this:

The size of this item is about 10mm x 2mm. I used a 1mm rubber tube as a connection 
point btw coil wire and output wire.

Nice ... but there was a short circuit with a coil core! I should have used better core isolation than acrylic paint. The mainplate is connected to the battery plus - so the coil will not work right.
In the following rewind process, I created a coil that didn't fit in the movement :(. I made too many wire layers.

The final working coil

In the final coil PoC (third), I didn't use rubber to connect wires because it was too big. I directly connected the coil wire and the output wire. I used glue to place the output isolated wire in the correct position. The output wire can be moved without damaging the silver connection point:

I used thin core isolation (school transparent tape) in the final working version. I also used glue to protect the coil wire.

Final PoC - self-made wire coil parameters vs genuine part: 

- lower electrical resistance, 
- bigger diameter,
- lower induction power due to lower  precision and wire length, 
- possible higher energy consumption. 

So, it doesn't look good on paper :). These are profound differences - the circuit board (chip) could be damaged. But I decided to install it - there's no other way and no sources of genuine parts...

The self-made coil has to be bigger than initially installed. Luckily there is some free space.

Because there is no original connector attached to the wire coil, I have to use a new screw on the right part of the coil handle (the original screw is much longer and covers a connector and watch circuit board).

The connection between the coil and the circuit board is made by enamelled copper wire. There is no space for wires covered with rubber. 

There is wire tension during an installation. Silver might not be strong enough to keep the connection between the output wire and the circuit board. I decided to use solder iron. This is the first permanent interference in the movement. I am not proud of it, but as I mentioned before, unfortunately, this watch came to me without the connector part. Much better would be to make (or buy) a proper connector  - but I didn't have enough patience at that point. 

And finally, movement is in one piece:

Under the "Swiss made" label, isolated output wires are connected with the circuit board and the silver connection points on the coil right handle.

It was a rather hope-driven development up to this point, without any serious calculations. I only estimated the number of required wire turns to create a coil. But it works. Video with working movement: 



Summary

- The chronograph module is very accurate and so far works without problems.
But there are side effects: 
- The coil induction power is reduced, so movement has to be in good condition and clean to work right.
- Probably battery will not last as long as with the genuine part (but after two months, it still works fine).
- It is pretty tricky and time-consuming to create a proper working coil of this size at home (I spend several evenings creating the first working coil).

Updates:

05.2022 - battery was replaced (old battery had been worked for 5-6 months), fixing connection issue between coil and circuit board (made by liquid silver).
06.2022 - I have replaced o-ring (now watch is also water proof)

List of tools used


Tools can be divided into two groups:

1. watchmaker tools (blue background)
- movement holder
- metal and plastic tweezers (a good quality number 2-3)
- watch case cushion
- rodico cleaning putty
- screwdriver set (a good quality watchmaker set with precise blades)
- watch hand lifting levers (I used a generic one - and I had to adjust it before I could use it without risk)
watch hand press set
- watch oilers
- case opener
- pegwood
- eyeglass
- glows
2. Additional tools for making wire coil  (black background)
- drill
- pin vise
- paper towel
- donors wire coils
- scalpel
- liquid silver
- Digital multimeter (resistance measurement)

External links

Great source about watch restoring, also about Jaeger-leCoultre/IWC calibre 630/1.

Jaeger-leCoultre calibre 630/631 data.

Info about IWC Schaffhausen Pilot's Chronograph ref. IW3740/IW3741

Mechaquartz watches and info.

Lavet-type stepping motor.

Rewind Quartz Watch Solenoid [thread]




Comments

  1. Impressive and a lot of patience. I have one similar movement but the chronograph does not reset to zero.do you know how to adjust ?

    ReplyDelete

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